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     This project was a failure. We ran in to a lot of obstacles along the way. The idea of this hydraulic arm was for it to pick up an object and move it. But it didn't work like we wanted to. Some of the problems we encountered were the middle joint wouldn't move up and down, the claw wouldn't open and close, and the tubing wasn't glued properly.

     Even though we encountered these problems we still kept going. I learned that I should glue the tubing properly and to have a better design for the arm. Also I learned never to give up even if I know that its not going to work.

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